DanielW
Well-known Member
- Location
- Haliburton, Ontario
This isn't anything fancy, but I was rather pleased with how it turned out. Last year I bought a Gleaner F for $390 that hadn't run in 20+ years. It was shedded for all that time though. I threw a carb kit in, replaced the alternator (which had stuck brushes) with a Delco single wire that I had kicking around, did a hasty tune up, and drove it the 4+ hours home (including a long stretch along the Trans Canada Highway on a busy tourist weekend - I didn't make too many friends that day...). Maybe not my wisest adventure, but all ended well.
The combine is surprisingly solid. Every auger and bin bottom was stored open, clean, solid, and tight (it would have needed to be maintained tight, as they used this combine for clover seed back in the day). All except the clean grain elevator, which they had somehow forgot to open, and which had sat for 20+ years in a dirt floor shed with a pile of crapulence in it. The clean-out door was rusted out and looked like a cheese grater.
Drew the pattern up in CAD, had the profile burned on the laser table at work, formed it at home (rather crudely) with a vice and using the drawbar of an old Cockshutt 540 as an anvil. And it fits like a glove. Still have to stitch he seams closed. I was out of MIG gas. I suppose I could have pulled out the stick welder, but 28 short stitches on thinner 16 gauge material is really more ideal for MIG. And I still have to stick a hinge on it. But it looks like it will work out dandy.
The combine is surprisingly solid. Every auger and bin bottom was stored open, clean, solid, and tight (it would have needed to be maintained tight, as they used this combine for clover seed back in the day). All except the clean grain elevator, which they had somehow forgot to open, and which had sat for 20+ years in a dirt floor shed with a pile of crapulence in it. The clean-out door was rusted out and looked like a cheese grater.
Drew the pattern up in CAD, had the profile burned on the laser table at work, formed it at home (rather crudely) with a vice and using the drawbar of an old Cockshutt 540 as an anvil. And it fits like a glove. Still have to stitch he seams closed. I was out of MIG gas. I suppose I could have pulled out the stick welder, but 28 short stitches on thinner 16 gauge material is really more ideal for MIG. And I still have to stick a hinge on it. But it looks like it will work out dandy.
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